Rotators and thrust bearings

 

Antenna use has grown with our station capabilities here. We currently use seven different antennae here. On this small city lot, it has presented some challenges. Here are some of them-

 

 

I have a couple of self imposed limits too:

 

 

Given these limitations, it was decided to locate an antenna rotator on the top of the house, as close to the center as possible. It took four iterations to get to where we are today.

My sweet wife is very understanding of my hobby. She has few requests and they have all been extremely reasonable. Since I have no wish to test the limits of this understanding, and I also have no wish to discuss ham radio with city code officials, I wanted to build a rotator that suited my needs and was as discrete as possible.

 

I put up my first Cushcraft 2 meter 4 element boomer on a TV antenna rotator strapped to the chimney in 2006. I later added a loop for 6 meters to the gable end on the left. It’s tough to see in the photo below. 

 

Let's call this Rotator 1.0, 2 meter boomer on chimney w/ TV antenna rotator. Probably taken in 2006, maybe early 2007. On the left is a 6 meter loop.

 

Our chimney is very loose to begin with. It’s not fall-off-the-roof loose, but a spalled bit of brick landed on a neighbor once. I’ve since put a new top on the chimney and it has two bands around it to hold it together. The chimney is not a good candidate to hold up an EME array, however. I think that has to be true in any house near this age.

 

There were problems from the start. The antenna flopped up and down several degrees vertically in one rotation. Partially due to the rear antenna mount, but partially because the rotator and mast are inadequate even for such a small antenna. The bracket and straps simply could not hold the antenna still. Using this antenna quickly demonstrated to me that I wanted a larger one and I knew that the rotator would have to be improved to handle it. I also hoped to be able to have more than one band on the rotator. At this point in my evolution, I didn’t even consider a 6 meter antenna on the mast. I thought it would be too large. I had been looking at how this problem is solved for folks who have towers, and learned that the rotator sits inside the tower and side thrusting on the rotator is braced by having a thrust bearing at the top. These forces would otherwise quickly damage a rotator holding up a large mast.

 

Below is a photo of the next setup being built and then up on the house. The frame and bearing of the rotator are made of treated wood. I used another piece on the side to hold the bearing in place. The bearing is screwed and glued to the back board that also mounts the TV rotator. I used a hole saw and made a nice oversize hole for the mast to go through. The back board was fastened to the house with 2 pieces of square tube screwed to the fascia board. In this house, that’s 1’ pine boards that are about 100 years old. I screwed the brackets in twice on each end. Galvanized was used for most hardware.

 

The antennae at this point were a 10 element 432 cushcraft and a Hy-Gain VB-214FM. This was a low budget operation.

 

The mast being built is on the left. A photo of the installation is in the middle, and on the right is a photo of the rotator after it was removed.

 

Rotator 2.0

 

While this was fun to make, it never worked as well as one might have wished. The TV antenna rotator only ever rotated about 330 degrees, and was always off by about 15 degrees. I even bought a new rotator for this attempt. Nevertheless, it was in use for a year.

 

I wanted to continue to use a TV antenna rotator because they are cheap and readily available. After all, a small bunch of antennae are not much bigger than a big honkin’ TV antenna anyway. Besides the rotator, I thought the wooden bearing surface must be the next thing that could be improved upon. I decided two bearings would be better, that way the motor could almost float and highly accurate alignment of the rotator and bearings would be less important.

 

Here is the third version after it was removed:

 

Rotator 3.0

 

The rotator above was made of stamped galvanized angle stock from the home improvement store (Menard’s). The bearings float on brackets and are made out of slippery nylon-plastic like cutting board. After they were aligned, I tightened them. They were cut slightly oversize with a hole saw and the rotator was mounted below in a slotted hole arrangement to make alignment easier. This rotator worked about as well as the first. Maybe less well. The flex in the frame skewed the bearings and they worked more like brakes. Since the brackets were made of aluminum and the frame of steel, this unit could not be welded to hold it together more stiffly. During the year this rotator was installed, we dashed the stucco on the house. The green buildup you see in the photo is overspray. You can also see how some of the hardware rusted very quickly, and some held up.

 

The fourth version (below) has been in use for three years now and works well. I was forced to give up on the TV rotator, so I bought a small Yaesu rotator and built the frame around it. It is about twice as big as the previous one. A friend of mine gave me a sheet of the decking he used in his snowmobile trailer. It is similar to the cutting board material, but it’s ½” thick. The frame was made from the same stamped galvanized angle stock, and was bolted together as a prototype. Then I installed the rotator and built a sleeve to adapt the mast size to it out of galvanized water pipe and other bits and pieces to shim it to size. Than I removed the unit and welded it, removed the nuts and bolts (to reduce weight) and painted the frame. I reassembled it, got it rotating properly and installed it with my neighbor. This one has the long side of the frame parallel to the house, as opposed to perpendicular in the last version. This was intended to minimize any sagging in the future. You can see I also added two more pieces of stock to hold it to the house. I inspect it every spring and fall and it has held up well. When the weather is below zero, or we have had freezing rain, it will sometimes refuse to rotate, but that might be true with any setup.

 

Rotator 4.0 This was taken sometime in 2008-2009

 

In Fall 2010 I noticed that the 2 meter antenna was beginning to sag. The birds had carried away the string I used to hold it up ( It is still the VB-214FM, which has a terrible bracket in the middle) so I decided to go up and repair it in an attempt to get a few more years out of it. One of the downsides of the arrangement we have here is that it’s inaccessible in the winter due to snow. I have a ladder that lays on the roof (an inverted v shaped thing that goes over the peak) to access the antenna without causing too much wear on the shingles.

 

For a ham living in the city with lots of wires everywhere, this is a good solution. It’s about as tall as I can get it. Using the house rather than a tower keeps the costs down. Not to mention, the feedlines are somewhat shorter too. There are a few disadvantages though:

 

 

Left bottom: DS rover yagi for 222, right bottom: DS rover yagi for 432, middle: DS 4 ele for 6m, top: Hy-Gain VB-214 FM.

 

 

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