Rewinding Kenpro KR-500 Elevation Rotor Motor

History

I have a Kenpro KR-500 Elevation Rotor that the motor burned up in due to a software malfunction of the control software.  The Kenpro does not have any limit switches, but just stalls when hitting the stop in the rotor.  The software moved the rotor past the zero point until it stopped moving.  This stalled the motor and before I realized what was happening, the motor burned up.  Kenpro sold out to Ysaeu back in the seventies and Ysaeu produced the elevation rotor under the model number of G-550, but it has been discontinued.

I searched the Internet for either a replacement rotor or some information where I might find a replacement motor.  No luck.  The prices were too high on the ones I found and I could not find a replacement part.  I called Ysaeu and after being passed from one person to another, I was told they couldn't help me.  In my research I happened on a web site by KB5WIA where he showed rewinding a motor for the Ysaeu G-5500 combination rotor.  The motor looked very similar to mine, so with some of the information from his site, I decided to make the attempt to rewind my rotor motor.  The following is a pictorial of the result.

Rotor Motor
The bad motor removed from the rotor.


Motor disasembled
The motor disassembled into its three main parts.

Motor
The motor plate and connection wires removed.  Notice the mark on  top right side of core.  This marks where the connection wires were run.

Core pins removed
I had to grind off the heads of the core pins to be able to remove the laminations.

Core lamentations removed
Wow!  It took a long time to remove each lamination, but I finally got it done.  I wonder if that was necessary.  More about that later.

Core, coils seperated
The motor core separated into outer, inner, and coils.  Notice the coils are numbered, so I can be sure an put them back in the same order.  Necessary?  Probably not, but I didn't want to take any chances.

wire removal
I purchased a winding machine off of ebay.  It was around $40.00 shipped.  I figured that was much better than trying to build something from scratch.  In the picture above one of the coils is now positioned to remove the old wires while counting the number of turns on the coil.

wire winding direction
I marked the direction that the old coil was wound, so I could be sure and wind it back in the same direction.

156 turns
Interesting!  On KB5WIA's web page, he says there was 158 turns on the coils he unwound.  I unwound three coils and came up with the same number of 156, so that's the number I decided to use.

156 turns back on
156 turns back on and Scotch 33 tape covering the coil wire.  Notice the setup.  I used my fishing real spool winder to hold the wire.  In the back you can see the new wire  The red arm device at the bottom of the spool is used to keep the spool from unwinding and hold a little tension as you wind the coil.

4 spools
All four coils re-wound and ready to be re-installed.

Resistance check
I checked each coil to see if they were about the same resistance value and they are.

Houston we have a problem
HOUSTON, WE HAVE A PROBLEM!  After installing the new coils on the inner core, I tried to start re-installing the laminations, but THEY WOULDN'T FIT!  Why?  What did I do?


Auh
I didn't realize that as I re-wound the coils, the edges of the coil forms were forced out; thereby preventing the laminations from going back on.  I don't know if  KB5WIA had this problem or not.  I don't think so because he probably would have mentioned it.  It would have been nice if he would have had the problem and mentioned it, I wouldn't have made the mistake. I now know better and hopefully it will help someone else who might wish to do a re-wind job on their rotor motor.  Notice in the picture above:  The coil on the right is one that I wound the first time and the one on the left is one that was wound using the method as described next.  You can see how much the right one is distorted.

re-winding the coil
After much deliberation, I decided to unwind the coils, and rewind them with the method described next.  I used an empty fishing line spool to roll the old wire off on to.


New coil rewind
Here is a finished re-wound coil.  Notice the large flat washer on each side of the coil form.  This prevents the coil form from distorting when being rewound.  But, because it also makes the diameter of the coil a little larger, I was not able to get all 156 turns back on.  I  had to take one turn off.  Too bad I didn't notice what was going on in the beginning, so that  I would have been able to put all the turns on..  The question is now, will it still work with one less turn.  I think it will, but we will have find out  further down the story.

Finished motor core
All four coils have been rewound and installed on the inner core.  The laminations will now go back on as they are supposed to.

finished motor
The motor has been re-assembled and mounted on the gear works.  Notice the thermal switch mounted on the side of the motor as was also done by KB5WIA.  It is rated to open at 70C.  The tywrap that is holding it on is rated for 85C so it should trip the motor off before it reaches the melting point of the tywrap (I hope) and therefore protecting the windings that are rated at 150C.

Well, it's come down to what we use to call the "smoke test," a term I hated when I was working for a living.  The following video is of the final test after assembly of the rotor.

Video:Smoke Test

A Short Video Of The Antenna Array In Operation Tracking Fox-1B In The Eastern Sky

Bottom Line

Lessons learned

I think I could have built a jig and pressed the outer core off the inner core assembly using my hydraulic press.  I didn't want to try it because I didn't want to damage the motor if it didn't press out easily.  If you decide to rewind your motor, you will have to decide for yourself to try and press off the core or disassemble it the way I did.

You should be careful not to distort the coil forms.  This means you will have to have some way to keep the forms from spreading.  I used a couple of big washers on the sides and it seem to do the trick.

Final Costs

Coil winder(I can use this again)  $42.30
Wire (I still have 800 feet left)     $19.49
Thermal switch                            $4.67
                                    Total     $66.46

I'm ready for the next time!