Heathkit Spares and Repairs

Heathkit spare parts are increasingly difficult to obtain now and the SB-Line units were made in the 1960s so some lateral thinking is required to find solutions for broken or worn out parts.


1. Control knobs

The transmitter loading and bandwidth control knobs on the SB-101 and similar units frequently breaks off where the lug meets the body and there are at least two different types - one with an Allen type grub screw and one with a pre-formed slot to fit over a shaped drive shaft.  The photo below shows both types with my repairs on the right. I filed the broken stub down flat and drilled a 1/16th inch (1.6mm) diameter hole through the centre of the stub and inserted a 10BA countersunk brass screw and a miniature switch spacer. A small amount of epoxy cement will be used to add some strength where the thread shows on the inner part of the body.

2. PA Tune Insulated coupler


These frequently crack, often due to being over-tightened. I have yet to find a solvent based adhesive that will work with the plastic that was used.


One option might be to find a piece of brass tube that is a tight fit over the coupler to use as a strengthening sleeve at each end with a clearance hole in each for the grub screw. The outer diameter of one sample was 0.503inches or 12.776mm.

3. Preselector and PA Loading O Rings


Almost every SB/HW unit that I have seen has O rings that are perished beyond reasonable use. They can be replaced with dial cord and a spring but the O rings are more convenient and are available at a reasonable cost from a Heath spares supplier in the USA. Three O rings are required, two identical smaller ones for the preselector and one larger one for the PA loading control.


As near as I can measure they are made of a solid circular materail of 0.14 inch diameter and the inner diameters are 2 inches and 2.5 inches respectively.

4. Dial Vernier Adjuster


Most of my SB-line units have problems with this part in that they do not grip the clear plastic dial properly. One solution might be to lift the LMO assembly vertically to push the wheel further on to the plastic but this is not easy with the filters obscuring some of the LMO fixings. In the end I decided to make some new adjusters with larger diameter cheeks and this seems to work much better. Ideally the cheeks should be made of thin phosphor bronze or beryllium copper but Ihaving none of those I used thin tin plated steel and set the cheek spacing to 0.052inches which is about 0.008inches smaller than the thickness of the plastic.


The shaft of diameter 0.123 inches was cut from a retaining bolt from a wafer switch which was exactly the right diameter to fit the dark green front panel moulding and only tapped for a very short distance.

The original is on the left and my new one is on the right. The fixing nuts have been locked with varnish and two washers have been fitted to the front of the shaft to space it off the plastic moulding.